1. Sound was bad from infamous switching 1/4" receptacles so disassembled extracting mainboard/output_pcb. Retensioning and contacts DeOxit cleaning achieved zero ohms reliability of normally closed switches. Retensioning involves removal of barbed soldertails switching contacts, bending and reinstall.
2. Also epoxy filled replica stem on reverb pot (sheared off), required removal and reinstall of pot, for gravity fill into cylindrical well created by blue painter's masking tape.
3. Used Molex pin extractor tool to increase tension female pins (downsize hollow). Used carbide needle pin to tension male pins (upsize nozzle). This imparted undue force onto motherboard pin solder joints causing cold joints. Jumper harness(s) molex pins exempt. When motherboard reassembled and tested, no speaker fiducial background noise (nil dc, nil ac, speaker spades, continuity good back to mainboard soldered molex pins). Mainboard then removed and found cold solder aforementioned, and repaired. Ground of AC power amp rails was lifted (XFMR CT) during initial energized trial. Could this have blown the TO3's (limitation voltage differential exceeded, base to emmiter)? I ask because post cold solder correction, still, speaker no fiducial background noise (nil ac, nil dc, across speaker spades). Speaker (and capacitored horn) is good.
4. 1988 schematic (all opamps index point towards rear channel heatsink) specifies different TO3's (SJ6392, SJ6505) then actuals in place (both Motorola with Motorola numbers, factory originals Peavey). All plus minus DC rails proper (46.5, 25, 16), there is no heat (very mild heat on sandblocks DC rail reduction), and DC rail is present where tracings distribute.
5. Confused. Send audio signal into front end input and confirm presence at preamp out?
6. Thanks in advance. Performing musician gave it to me and I want to give it operating, to my church worship group.
2. Also epoxy filled replica stem on reverb pot (sheared off), required removal and reinstall of pot, for gravity fill into cylindrical well created by blue painter's masking tape.
3. Used Molex pin extractor tool to increase tension female pins (downsize hollow). Used carbide needle pin to tension male pins (upsize nozzle). This imparted undue force onto motherboard pin solder joints causing cold joints. Jumper harness(s) molex pins exempt. When motherboard reassembled and tested, no speaker fiducial background noise (nil dc, nil ac, speaker spades, continuity good back to mainboard soldered molex pins). Mainboard then removed and found cold solder aforementioned, and repaired. Ground of AC power amp rails was lifted (XFMR CT) during initial energized trial. Could this have blown the TO3's (limitation voltage differential exceeded, base to emmiter)? I ask because post cold solder correction, still, speaker no fiducial background noise (nil ac, nil dc, across speaker spades). Speaker (and capacitored horn) is good.
4. 1988 schematic (all opamps index point towards rear channel heatsink) specifies different TO3's (SJ6392, SJ6505) then actuals in place (both Motorola with Motorola numbers, factory originals Peavey). All plus minus DC rails proper (46.5, 25, 16), there is no heat (very mild heat on sandblocks DC rail reduction), and DC rail is present where tracings distribute.
5. Confused. Send audio signal into front end input and confirm presence at preamp out?
6. Thanks in advance. Performing musician gave it to me and I want to give it operating, to my church worship group.
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